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HomeMy WebLinkAboutWelding Inspection Report 01.19.2017STC Welding Inspection Report Steven T. Conway (CWI) 4663 W Rd. DeBeque, Co 81630 970-618-1624 Contractor. Smith built Inc. ( Steel Cont. Roger Grove) Phone: 970.379.8861 Job Name: Zurcher ADO Cottage Contractor Contact: Bridger Smith Phone: 970.379.9400 Permit Number: I, WORKING CONDITIONS Weather Condltlona: Cold and Dry. Below 32 Degrees Date: 1/1912017 CONSTRUCTION WELDING PROGRESS Reference Drawings: Weldament Identification & Location Bolts Inspected Detail Sheet Grid Loc. Column Sheet Grid Loc. 111: I inspected 85% of all bolts installed after installation. To the right of this L (S5.0) S2.2 A & 2.2 text is approximant area bolts NOT of inspected. Bolts used for 15/16" TCB's. Visual inspection only for T (S6.4) L. (S5.0) S2.2 S2.2 B & 3 H -F & 5 .steel to steel connection were Inspected. tf3olts 2: I found two TCB bolts untorqued at these locations. Contractor did not L (S5.0) S2 2 F & 4 have a snap aun at the time. Rodger Grove assured me he would get them no notice to verify later. It was a column i snapped et a later time. 1 received in beam connection. Location to the rht of this text. - f) .. Technical Yes No NA Yes No NA 1: Percentage of Bolts inspected Recorded x 11: All details reviewed by Inspector x 2: Type of Bolts inspected Recorded x 12 Proper procedures performed during Installation x 3: Inspection procedure recorded x 13: Any rework due to misplacement or wrong sizes Inslalled x 4: Location of Bolts inspected x 14: Any rework ordered due to none conformance x 5: Continuous inspection of epoxy Bolts x 15: Al! Inspected Installs satisfactory x 6: Continuous inspec.of Reinforcement dowels x 7: Type of epoxy used was recorded x B. Ambient temperature recorded x 9. Depth varied and recorded x 19. Other _ ,10: Hole sizes verified and recorded x Remarks: As requested a special inspection of bolts was conducted per IBC 2009 Chapter 17: Structural Tests & Specie] inspection. A visual bots Inspection was conducted on most of the TCB's in the upper connections. Mostly Column to Beam connections es that was all that was visible for the most part. See upper portions of IhiS report for derails. Lacalions f on this report was taken from the structural drawings provided by Studio M Engineers 308 N. Hyland Park Or. Glenwood Springs, CO. 970.366.8690. See "technical" _provided section this report. As stated there were two TCB twits that 1 found not snapped. Roder Grove did not have a snap gun available today. I could not verity that those bolts were Eightened to_propar tension. See the " Bolts Inspection portion above Tar details. if there are further questions or additions needed per this report please feel free to contact me. !!!!!!!!����.... Steven T Conway 11ft C W 114043221 tit OC1 EXP. 4/1/201i Inspector's Signature: Steven T Conway Date: 111912017 Mileage: 0 Hours: 7 b